[关键词]
[摘要]
以某燃气轮机低压8级压气机为母型,开展加零级改进设计。通过对母型机进行分析,合理地选取匹配点,对压气机零级进行了一维、二维气动设计,最后对零级压气机叶片进行三维造型。数值结果表明:新设计压气机在设计转速7 450 r/min下,流量为123 kg/s,总压比为6.125,等熵效率为88.3%,喘振裕度为32.8%,达到了设计指标;新设计零级与母型机流场匹配较好;通过对压气机变工况性能进行分析,各主要运行工况喘振裕度满足10%设计要求。
[Key word]
[Abstract]
Based on the prototype of a marine gas turbine 8stage low pressure compressor,an innovation design with zerostage addition is carried out.After analyzing detailed and selecting reasonably the matching point of the prototype compressor,onedimensional and twodimensional detailed aerodynamic designs for the zerostage are conducted.At last,the threedimensional modeling is also used for the zerostage blade design.The new design 9stage compressor numerical results show that the massflow is 123 kg/s,the total pressure ratio is 6.125,the isentropic efficiency is 88.3%,and the surge margin is 32.8% at the design speed of 7 450 r/min.All of the results above meet the design target.The flowfield of the front zerostage matches well with the rear prototype compressor stages.The Analysis on the offdesign performance of the new compressor indicates the surge margin of main operating conditions also meets the design requirement of 10%.
[中图分类号]
TK473
[基金项目]
航空发动机及燃气轮机国家重大科技专项;船舶与海洋工程动力系统国家工程实验室——海洋工程燃气轮机实验室资助项目